Turbo 350 problem

Collapse
X
 
  • Time
  • Show
Clear All
new posts
  • meatwagon

    #1

    Turbo 350 problem

    Having problem with a tranny. When it's cold at a stop it starts off in first, no problem. When it's warm at a stop it tends to start off in second (it will manually shift into first). The vacuum line to the modulator is good and there's no tranny fluid in the vacuum line. Is the modulator going bad? Any suggestions are greatly appreciated
  • SpiderGearsMan
    No Life Outside BangShift.com
    • Oct 2007
    • 22359

    #2
    Re: Turbo 350 problem

    do you have your kick down cable attached ?
    the other day we noticed a real non "C" th350 has not been made in 31 years
    time flies

    Comment

    • IndyShiftman
      Superhero BangShifter
      • Dec 2007
      • 1122

      #3
      Re: Turbo 350 problem

      If you have a vacuum gauge, check the vacuum at the modulator when its warm. Should have good vacuum and it should drop when you rev the engine.
      Then if you have good vacuum and it fluctuates, take the governor out and check the valve inside by holding the gov upright with the gear pointed straight up and push the weights in. You should be able to see the valve inside move up and down. If it's stuck that's your problem. But if it's stuck due to debris then you may have a internal problem. Drop the pan and check for debris. Then overhaul if needed,

      Also about the gov. The gear should be in good shape. Not worn down in the middle. And the shaft shouldn't fit loosely in body that has the weights.

      Comment

      • meatwagon

        #4
        Re: Turbo 350 problem

        Had a kickdown cable and it felt "spring-loaded" so I'm assuming it's functional. When I see the car again I'll test the vacuum and pull out the governor and check it like Indy suggests. Thanks, guys.

        Comment

        • IndyShiftman
          Superhero BangShifter
          • Dec 2007
          • 1122

          #5
          Re: Turbo 350 problem

          It should take off in low even if it didn't have a kickdown cable.

          Comment

          • Caveman

            #6
            Re: Turbo 350 problem

            On the TH350 in my '56 pickemup, the kickdown cable plastic thingy that bolts onto the case was leaking.....

            So I cleaned it, and investigated. Turns out it was loose.... because the bolt had stripped out. *&^%$#@!!!

            So I cleaned it up, put some red RTV on the threads and under the washer, and gently put it back in.


            Indy, is my case now crap, or can I just drop the pan, drill it out, and re-tap it with a slightly larger thread bolt?

            Whats underneath that bolt-down spot? Can I just drill it a 1/4" deeper and tap it and use a longer bolt?

            Comment

            • joe_rocket45
              Superhero BangShifter
              • Nov 2007
              • 1098

              #7
              Re: Turbo 350 problem

              a way to cheat that stripped out hole...
              stick the small end of a zip tie in the hole and thread the bolt in, works about 100 times better than silly-cone

              Comment

              • IndyShiftman
                Superhero BangShifter
                • Dec 2007
                • 1122

                #8
                Re: Turbo 350 problem

                Originally posted by Caveman
                On the TH350 in my '56 pickemup, the kickdown cable plastic thingy that bolts onto the case was leaking.....

                So I cleaned it, and investigated. Turns out it was loose.... because the bolt had stripped out. *&^%$#@!!!

                So I cleaned it up, put some red RTV on the threads and under the washer, and gently put it back in.


                Indy, is my case now crap, or can I just drop the pan, drill it out, and re-tap it with a slightly larger thread bolt?

                Whats underneath that bolt-down spot? Can I just drill it a 1/4" deeper and tap it and use a longer bolt?
                Sometimes a slightly longer bolt will catch good threads in the bottom. Just be sure not to over tighten.

                Comment

                • IRONHEAD

                  #9
                  Re: Turbo 350 problem

                  Originally posted by joe_rocket45
                  a way to cheat that stripped out hole...
                  stick the small end of a zip tie in the hole and thread the bolt in, works about 100 times better than silly-cone
                  X2

                  Comment

                  Working...