The problems for the Angry Grandpa Chrysler started on the last day of the PRI show. As Lohnes and I were getting our cars warmed up in the morning before heading over to the convention center, two very similar Chrysler products were having two very different mornings. His rental 5.7L Dodge Challenger was thumping along at idle, nothing wrong. AG, on the other hand, was suddenly in full-panic mode. No, wait a minute…that was the owner. The oil pressure had read flat zero, the check-engine light was going berserk and my heart was in my throat. After a bit of panicking and more than a few minutes of troubleshooting, it was determined that my oil pressure sender had cracked just shy of 150,000 miles, spitting enough oil to not read on the dipstick and not sending a pressure signal. I figured that I had dodged a bullet, so with fresh oil poured in and a friend following me home, I limped the car back home to Bowling Green, changed out the sensor, and was all ready to start driving the car again. That’s when things got worse…not only was I not getting a pressure signal, now I wasn’t getting an oil temperature signal and the computer was having a fit. Another teardown revealed that the female connectors for both sensors no longer locked in place, their locking tabs broken clean off. There was no way that a signal was going to the ECM.
That meant that I would have to get new female connector ends and splice them onto the existing wiring harness. No issue, right? Wrong. Because the 300C is over ten years old, supplies are starting to dry up at dealerships and in the case of one connector, was discontinued by the supplier. The reason why Angry Grandpa spent about a month parked in mothballs was because I was hunting down those connector ends…junkyards proved fruitless and eventually, I had to turn to some pros in the business. Thanks to Andy at EastCoastMoparts.com, I was able to track down the discontinued item and my local dealership was able to pull in the other. They were not cheap, but electrical hardware isn’t something to cheap out on.
Many people cringe at the idea of rewiring something. Lucky for me, electrical work isn’t all that bad. For years part of my job as a helicopter technician involved connector setups in the same vein as these. Compared to pinning cannon plugs for a Kiowa, the connectors for the Chrysler were a breeze. Here’s how the work went down in the shop…nothing is too complicated, the hardest part of the job is removing the alternator to get to both connectors and the most specialized tool I broke out was a pair of crimping pliers that you can pick up from pretty much any hardware store or auto parts store. All in all, including breaks to warm up (it didn’t break twenty degrees outside today) the whole process took me two hours, from the moment I started ripping off the belly pans to the moment I fired off the car and verified that there was no more check engine light…or pig-rich idle.
Anchor brand connectors can be had with hot melt glue in them or I sometimes use silicone sealant in the heat shrink when working on my boat. Modern connectors can be a pain.
Solder is your friend. I solder all my crimps.