Took it to the Underground Garage yesterday and put it in the @UGGdyno. Base line pulls were in line with last time. Pulled the cap on the exhaust dump and it made 3 more HP very disappointed. Looking at the logs I had some very aggressive timing retard so the on more pound of boost it made pulled timing.
Changed to NGK plugs and tired to make heads and tails of the timing mark. The white part of the mark was over the bend a little. One pull we got a little black about half way across the top. Assuming that the timing mark. I am calling it close enough. Started asking Holley to give me more boost ended up with About 15 psi / 18° and 450 rwhp! Was hoping to see 425, added flex fuel and more boost and it pick up 100 rear wheel!
Planning on taking it to the track tonight. Fingers crossed
Changed to NGK plugs and tired to make heads and tails of the timing mark. The white part of the mark was over the bend a little. One pull we got a little black about half way across the top. Assuming that the timing mark. I am calling it close enough. Started asking Holley to give me more boost ended up with About 15 psi / 18° and 450 rwhp! Was hoping to see 425, added flex fuel and more boost and it pick up 100 rear wheel!
Planning on taking it to the track tonight. Fingers crossed
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